View Single Post
      06-16-2019, 11:22 AM   #77
jandref321
Captain
jandref321's Avatar
346
Rep
728
Posts

Drives: 2012 X5M
Join Date: May 2014
Location: United States

iTrader: (1)

I finally got the chance to work on the car...it appears that my misfire issue was the JB4. I looked over the wiring several times, and there was no issue. I'm unsure if it was a firmware or hardware issue with the unit. I ended up pulling it out entirely and will look it over again when I get the chance to see if something needs to be soldered. The truck is running perfectly now.



I also replaced the filtered air ducts again, since mine were ghetto from the catch cans I had installed and then removed. Honestly, I was getting more oil in the systems with the catch cans than with the stock hoses anyway. I haven't gotten a boost leak code yet, but I also haven't driven it hard. I'll have to see if I can put it under load. The problem I have now is that I don't have a system to log and check boost without the JB4. I tried the torque app, but I couldn't get it to operate accurately...I'll have to look around for something else before going back to P3.
__________________

2020 G01 X3 30e CURRENT M Sport Package
2019 Ford Raptor SuperCrew CURRENT 802A, KN Drop-in, RB Flaps, Husky Well Liners
2012 E70 X5M SOLD Stg 1+ Turbos, DPs, Velos Stg 2+, JB4, Race Cats, Bavauto Coils
2003 E46 M3 SOLD aFe CAI, AP Axleback, SSK, H&R Springs, TMS CMBR Arms, PF RTABs
Appreciate 0